The plan
was to take a genuine Turbo Technics 205GTi and upgrade it
to an Emerald ECU. This could have been a really easy conversion,
but we decided to complicate matters with a few more upgrades!
The easy
way to convert the TT205 to M3DK would have been to retain
the distributor. Pug distributors are not known to be the
most reliable of units, but there is a simple fix. Take a
VW Golf 1800cc 16v Hall Effect distributor (Bosch unit) and
clip on a distributor cap from the Vauxhall Cavalier. This
lot bolts to the 205 and then you can retain the original
HT leads.
We decided to upgrade to distributorless operation
and use the late GTi flywheel and crank sensor. This gives
you a 60-2 trigger directly from the flywheel and a factory
reliable pick-up sensor. Obviously t his means removing the
gearbox to fit the flywheel and that’s where it all
started to get complicated. Armed with the “book of
lies” (aftermarket manual) we started by making up a
small section of tube to hold the diff in place once the drive
shaft had been removed. In the event this tube fell out several
times during the week and it seemed to make no difference
at all but we felt the need to follow the book.
The original TT conversion uses an additional injector in
the end of the throttle body to add the necessary extra fuel.
The standard management takes care of the fuelling the rest
of the time. The fuelling requirement is determined by an
air flow meter in the stock setup but the Emerald unit only
requires a throttle pot and a Manifold Air Pressure (MAP)
sensor. This allowed us to junk a lot of the original
clutter from under the bonnet and just pipe cold air to
the intake via a suitable cone filter. The extra injector
went out the window and we fitted a set of injectors with
a larger flow capacity. These were borrowed from a late Mini
Cooper (breaker’s yard job) but see the injector feature
elsewhere on this web site for advice on injector selection.
We had a problem in as much as the new injectors were shorter
than the originals. The answer was to turn up some stepped
spacers with o-ring seals to close the gap. The easier way
would have been to find the right length injectors!
While doing
all this work we found something of a bonus - a fully ported
cylinder head!
On the wiring front we had little choice but to start pretty
much from scratch. The original system is fuel-only with clockwork
advance so we rewired the car for the crank sensor, MAP sensor,
throttle pot
and
twin coils plus boost control valve. All the pin outs are
in the manual along with a generic wiring diagram. To fit
the pot we had to make up this adapter bracket.
While we were at it we decided to remove a lot of redundant
wiring. Someone had previously fitted an alarm system (wires
all the same colour)
but the alarm was missing when we bought the car. This was
later to prove a real headache but at the time it seemed like
a good idea!
The TT system used a two-position switch for high and low
boost. Low boost is about 6/7psi and high is up to 10/12psi.
The manifold design is such that you get very fast throttle
response but at the price of high manifold temperatures. We
drilled out the outer studs in the head at the exhaust manifold
flange and increased the stud size to 12mm as per the original
TT upgrade. There had been problems apparently with the manifolds
distorting due to excessive thermal load.
The coil pack we used was from a Ford Zetec engine
and we had
to adapt the HT leads to suit their connectors. This involved
a bit of DIY cutting and shutting but in the event it wasn’t
too successful. We have since ordered up a custom set of Magnacore
8mm leads.
The ECU can control boost pressure but we thought we were
lacking the right valve for the waste-gate. For the time being
we planned to just set the boost on the operating rod. The
right valve was to be added later on. As it turned out we
could have retained the original Turbo Technics valve and
just plumbed it in differently. As it was we ended up with
the Audi TT valve.
Not part of the master plan was the need for new discs and
pads plus drive
shaft boots. It was all getting a bit above budget when the
service items like engine oil and filter were added on.
The M3DK has a small LED on the lid which lights red when
the ECU is live. This turns green when the box sees a cranking
signal. It’s a quick way of telling if the system has
power and is seeing engine cranking. All was well, and prior
to starting we cranked up the oil pressure with the spark
plugs out. The motor burst into life pretty much straight
away but we had to call a halt to the warm-up due to a massive
oil leak! After much messing about we realised that the new
filter was leaking at the seam. I’ve never seen that
before but it was late and we were in time trouble already.
A dive into the rubbish bin rescued the old filter and this
was cleaned out (as well as we could) and re-fitted.
With the oil leak cured it was a case of mapping the engine
on the rolling road. We had taken a power curve before starting,
on both high and low boost settings. We were over the moon
about the results. We now had better torque and slightly more
power on low boost than the engine previously had on high
boost! We had yet to fit the control valve to map the boost
pressure but it was looking good.
Not so good was the rain outside the workshop and the electric
windows that would not wind up! When we removed all the redundant
alarm wires we lost the electric window winder controls. It
took a lot of finding but eventually the windows closed.
Red
Hot
More of
a worry was the turbo temperature. After one power run the
turbo was glowing red hot. This isn’t unusual but Richard
(the owner of the car) was really worried about it. He said
that while driving on the road he stopped a couple of times
to look under the bonnet and the turbo was glowing red hot
in the dark.
We have since fitted a thermocouple into the exhaust to monitor
the gas temperature. This reads out via an old tyre temp read-out
box which is powered by a PP3 battery. When the battery drains
down you get a false (high) reading – Richard knows
all about this because he lost a couple of years off his life
through worry - until he installed a new battery. Now he was
seeing maximum temperatures around 850°C which is fine.
When we map for maximum boost we may have to over-fuel the
turbo at higher boost pressures to keep the temperature down.
It will be interesting to see what sort of mixture ratios
we have to run to keep everything together. Fortunately with
the full engine management we have the facility to control
just about everything and we can now data log to keep a record
of what’s going on. Richard has already data logged
a series of cold starts to fine tune the cold running. The
software allows you to start/stop from any recorded function
so this was set to water temperature to avoid collecting too
much data. It starts anywhere below 20°C and stops at
70°C.
Maximum
boost
After a
couple of weeks running about on low boost the car came back
for the plumbing in of the boost control valve.
Basically this is a valve we robbed from an Audi TT/Golf GTi
1.8T engine. The valve leaks air from the pipe that goes to
the waste gate diaphragm. By bleeding air away from this pipe
the boost increases because the waste gate doesn’t open
when it would have.
The biggest advantage of this system is that you can map the
boost to stay fairly constant across the rev range. Obviously
you can’t demand boost where there isn’t any available
from the turbo - and if the turbo is running out of breath
at higher rpm then there’s nothing you can do about
it.
Our car originally made a little over 135bhp on low boost
and 160bhp on high. Now it is running 160bhp on low setting
and 190bhp on high with over 200ft lbs of torque. The problem
with the high boost setting is that the inlet temperature
is going too high (logged on the M3DK). We are seeing as much
as 70°C at high boost. What’s now needed is better
inter-cooling of the intake charge. The other problem is lack
of grip! The car is ridiculous in the dry and lethal in the
wet on high boost.
The turbo overheating isn’t the problem we feared it
might be but better charge cooling would be the next step
to even more power. Always looking for the most cost-effective
solution we are planning on making up an intercooler-sprayer.
This is nothing more trick than a windscreen washer pump spraying
water onto the intercooler radiator. The switching will be
controlled by the general purpose PWM output in the ECU on
a pressure Vs rpm map which also links to the air temperature.
This means that the pump only switches on to spray the intercooler
when both boost and air temperature are high.
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